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big prob, to much compression? only on one side?


bink98xcab

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ok heres tha problem i went for a ride today and tha shee died and backfired so i guessed i probly losat one cylinder and yes thats what happened i had 150 and 147psi and i was running 91 octane w octane booster, and blew a whole right through the center of one piston , but the other looks fine, is this to much compression for 91? i have 21cc domes at sea level , the topend has less than 5 hrs on it and has 64.5 pro lites. should i get 22cc's and replace the one piston? walls of cylinder feel fine . no scroring . any help would be egreat

 

http://i272.photobucket.com/albums/jj170/b...pg?t=1204236984

 

http://i272.photobucket.com/albums/jj170/b...pg?t=1204237038

Edited by bink98xcab
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so you dont think it was to much compression? the plug was brown yesterday and the plug was tight and i just had the carbs apart last weak and they wasnt any trash. im running k&n pods 340 mains fmf pipes noss head vforce3's , one of my buddies did this but his plug was about to pop out when the top went, so i knew his leaned out.

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I can't see the pictures very well but unless your timing is advanced a lot, you shouldn't detonate in Oklahoma with 21cc domes and 91 octane. I would run 93 octane if you can get it.

 

-David

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ok heres tha problem i went for a ride today and tha shee died and backfired so i guessed i probly losat one cylinder and yes thats what happened i had 150 and 147psi and i was running 91 octane w octane booster, and blew a whole right through the center of one piston , but the other looks fine, is this to much compression for 91? i have 21cc domes at sea level , the topend has less than 5 hrs on it and has 64.5 pro lites. should i get 22cc's and replace the one piston? walls of cylinder feel fine . no scroring . any help would be egreat

 

http://i272.photobucket.com/albums/jj170/b...pg?t=1204236984

 

http://i272.photobucket.com/albums/jj170/b...pg?t=1204237038

 

 

 

 

IMO 91 is too low for 150psi. Octane booster isnt gonna help either. Its a gimmick. It raises actual octane by like half a point at most. The only real octane booster is Torco.

 

 

However, looks like you really leaned out on that jug for some reason. If it was just octane both pistons would be affected. It has to really go seriously lean to melt a hole in a piston. You should have been able to feel it. It should have gave signs of leaning out.

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i gues il tear down the carb on that side after work tomorow to see if thats the prob , caus right now im stumped, and thanks for the help :banghead: the only sign of bein lean was right before it died when i gave it WOT and it wouldnt pulled hardley past 3/4 throttle

Edited by bink98xcab
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i gues il tear down the carb on that side after work tomorow to see if thats the prob , caus right now im stumped, and thanks for the help :banghead: the only sign of bein lean was right before it died when i gave it WOT and it wouldnt pulled hardley past 3/4 throttle

 

 

 

 

Yep. Did it sound hollow and boggy? Something happened on that carb and it completly lost fuel.

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well it only had that "holow , boggy " sound after i started it after it died, and then i knew what was up, but like i sade , right before it died it had that no rev , lean feeling, but BOOM it was to late and hadnt ever gave previous probs

 

 

 

I messed up my float heights last time I changes jets on my OKO's. Caused my bowls to run out. I caught it and fixed it before it did any damage that I know of. Might wanna check that.

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so you dont think it was to much compression? the plug was brown yesterday and the plug was tight and i just had the carbs apart last weak and they wasnt any trash. im running k&n pods 340 mains fmf pipes noss head vforce3's , one of my buddies did this but his plug was about to pop out when the top went, so i knew his leaned out.

Detonation can cause the plug to back out...

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I would make sure I did a pressure test on the motor when you get it back together. Had you checked the plugs at all after the rebuild and running it a bit?

oh yea i have checked the plugs after each ride , because i have been adding a few mods one a time , and i havent really had more than a couple rides each before the next mod. i planeed on checked the pressure after i get it back together. any one know where a good place to just get the rings? (pn# 2539cd) i ordered a piston off ebay but tha stupid thing dont come w rings!! i didnt realize till i won the auction.

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