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need help , everything new and still a pos


woodro77

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ok , rebuilt the motor ,top and bottom , brand new , mods are +4 timing advance , fmf fattys , k+n no lid , v -force reeds , tors removed , jetted with vitos jet kit w/ 300 mains , sea level , (ny) .

 

ran good when started up ,a little hard to start, bogs till warmed up, idled fine sounded good , first ride had a small bog at bottom end , (still new to banshee , heard they all have it ) about 15 minutes into ride started to bog down , then would hardly run at all , after 10 minutes sitting started up and seamed to run fine , brought it home , when cold a litttle hard to start , about 7 kicks , and bogs and stalls till warm ,

compression is still good.

 

is it possible for the jetting off , ( let it run good for about 10 minutes then to shit ) sounds like its loading up with fuel (if possible )

please help

 

just built this shee from scratch , about to part out if i cant get it to run good , (maybe 4 poke)dont want to but geting tire of working on this thing

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ok , rebuilt the motor ,top and bottom , brand new , mods are +4 timing advance , fmf fattys , k+n no lid , v -force reeds , tors removed , jetted with vitos jet kit w/ 300 mains , sea level , (ny) .

 

ran good when started up ,a little hard to start, bogs till warmed up, idled fine sounded good , first ride had a small bog at bottom end , (still new to banshee , heard they all have it ) about 15 minutes into ride started to bog down , then would hardly run at all , after 10 minutes sitting started up and seamed to run fine , brought it home , when cold a litttle hard to start , about 7 kicks , and bogs and stalls till warm ,

compression is still good.

 

is it possible for the jetting off , ( let it run good for about 10 minutes then to shit ) sounds like its loading up with fuel (if possible )

please help

 

just built this shee from scratch , about to part out if i cant get it to run good , (maybe 4 poke)dont want to but geting tire of working on this thing

 

sounds like some sort of fuel related problem. change the plugs, and make sure the gap is set properly. get it going, take it for a fast spin, then see what the plugs look like. That should tell you where to go on the tune. If the jetting is off that hould tell you. Is the gas new gas, or has it been sitting mixed for a few weeks? Did you get the carbs new or second hand? Take the carbs apart and clean them up nice.

 

What jets are in the bike now? If you have come so far it makes no sense to quit now.

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A 300 main seems rich to me I'm basically at sea level and I ran a 310 in the stock carbs with the motor in my sig gas mixed 40;1 klotz before that i had fatties and almost exact same mods as you and was at 280 main stock pilots needle 1 down from middle airscrew 2 turns out. What size pilot do you have in there? it jus sounds like your carbs are out of whack nothing big time. I'd say maybe run a 290 needle in middle clip with stock pilot or 27.5 airscrew 2 turns out try that and let us know.

 

Josh

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thanks guys i will try new jetting tommorro , will let you guys know how it works out

Could also be electrical. Resistance builds with heat. That could explain why it runs good until it gets hot, Then runs better when it cools.I have had that experience with both stator and coil.It sounds like your jetting it not quite either but that might not be the only thing wrong. You can test the stator and coil using an ohm meter. the specs are in Clymers. Check it while the bike is cold, and then again when it starts to act up.

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never going to believe this , cleaned carbs and took it for a ride again , 15 minutes and it died again let it cool down ran then died , while sitting there and thinking about just setting it on fire right where it sits , saw that the gas cap vent hose had a kink in it , took it off and it runs like a raped ape, starts on first kick , i cant believe something that stupid drove almost crazy ,

 

thanks for all your help guys ,

 

has this happened to anyone else ?

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has this happened to anyone else ?

 

 

i've seen a clogged tank vent cause it. i took my cap apart and removed the stuff like the little steel ball and such and put it back together.seems to allow for a better gas flow.however you must make sure you have a hose attached to the cap and that its long enough so water don't get in through the vent.

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hahaha well good news it was something so simple. How do you like it now?

 

 

i just raced my brother on his trx 450 with a cam and pipe and k+n , and beat him , not by much but i dont have many mods , pipes ,v force , k+n , +4 timing advance

 

 

im starting to like this banshee, going to take it in the sand tommorro , probably even better

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