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cheetah after math...


bigscary

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ok, after studying the pics a bit, from what I can see it looks like your wring spun, and caught the exhaust port. the gap in the wring isn't supposed to be against your exhaust port, should be to the side of it. Excessive wall clearance? I can only see 1 gap in the pictures posted, just some ideas for ya.. good luck.

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Since you have the piston in hand check this page and compare... http://www.mztech.fsnet.co.uk/workshop/wrk_piston.html

 

I think you got an air leak or lack of fuel in that cylinder. That caused the rest of the damage after the melt down.

 

What octane was that sunoco. Was it pump gas. Does the other piston show any heat damage... even under the crown.. like black marks underneath.

 

I think its the burn hole one in the pics on that page.

Edited by fixitrod
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You have gotten enough posts on Planet Sand  to help you with your problem... one word of advice though... Listen to Calvin since he's the one that makes those cylinders. Did you happen to warm it up before you hammered the throttle?

360545[/snapback]

 

 

yes I warmed it up well b4 every run.....

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Since you have the piston in hand check this page and compare... http://www.mztech.fsnet.co.uk/workshop/wrk_piston.html

 

I think you got an air leak or lack of fuel in that cylinder. That caused the rest of the damage after the melt down.

 

 

360306[/snapback]

 

 

Bingo!...classic detonation meltdown. Look at the melted material on the exhaust bridges. Also looks like the intake sides of the piston were trying to stick as well. Either lean mixture,air leak , clogged jet caused this. 220 lbs compression didnt help things either. Check the carbs, gaskets and drop the compression to something more reasonable...it might hit harder on the bottom with that much compression but it is almost certainly played a part in this and is probably slowing you down on top-end.....Jim

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after reading all of the coments, heres my theory......

 

the left plug vibrated out........and it continued to run cor about 1-2 seconds.....

sucking air through the crankcase into the right cylinder.......leaning the hell outa it......(Melt down begins)

 

it made it about 2 more runs b4 completely locking up......

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after reading all of the coments, heres my theory......

 

the left plug vibrated out........and it continued to run cor about 1-2 seconds.....

sucking air through the crankcase into the right cylinder.......leaning the hell outa it......(Melt down begins)

 

it made it about 2 more runs b4 completely locking up......

361489[/snapback]

anytime i ran over 185 psi i ran a plug lock....best $20 i spent.

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