The bike is an RD400 (air cooled) mild port, pipes, stock compression. Carbs are pwk 30mm (oko) needle is a GJH. When I originally started the bike I had 155 main jets. I put about 100 miles on the bike before I started running it hard. With the 155 it seemed very rich, didn't want to come on the pipe at all. 1 dropped down to a 150 and it got better but still wasn't 100% clean. Went to a 148 and it was clean and felt good. I put about another 300 miles on it, not running it too hard, while I dialed the needle in. Once it felt like everything was good, I wanted to make sure before I started adding timing. After the first plug chop I realized it was lean. I went up one size on the L and 2 on the R (150L, 152R) after I did another chop it seemed even leaner. I just got back from a third chop. I put 155 mains in just to see what would happen and it ran good. Didn't come on the pipe as violently but seemed like it pulled harder. I'm guessing it's still a little lean, but y'all have way more experience at this than me. I don't know why it wouldn't run before with the 155mj but does now. Either the rings weren't seated or the needle was way off to begin with (JJH). it seems like it's responding to a jet change now, so if it's still lean I'll order some more jets. Sorry if I'm talking in circles. Any advise would be greatly appreciated! Sent from my SM-G965U using Tapatalk