Update...took the bike to a bud, and found hella leaks around the cylinders, as well as possible spark issues, my cool wires were taped to the coil, and I had plug caps that didn't ohm to 5k, change those to NGK caps, changed my 1/8 barb end to a 1/4 end (hose end) as well as a new coil, and cylinder gasket.., shortened up hoses for the vacuum and fuel, took to the dyno right after, and got the high 97 ponies. Guess not to bad. Finally ran it Sunday, and it ran flawless. Thanks for the advice I received and shout out to my bud Sent from my LG-D722 using Tapatalk