I ran through all 6 gears and stayed in sixth for maybe 3 to 5 seconds, maybe I did not run long enough?.....As for the pilot I had it on a dyno and according to the machine my low end was too lean "52 pilot at the time" so I bumped it up to a 58 and still low end bog. It showed my top end was way rich "had a 175 in a the time" I would drop a size and try it and when I got to a 162 the top end ran great, so did the plug chop and it looked lean to me, so went back up and when you get to the top it feels like it wants to fall on its face sometimes. Before I had my case ported I ran a 155 main...45 pilot...cel on 4th clip...Would just porting the cases changed your jetting that much? Also at the time of the dyno I had DGH needles "Or DGK whatwhatever they are" in and clip was in bottom position so I changed them back to my cel in 4th position